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Member Page: Chris W

sweep Chris W

Chris W

Member ID: sweep
Member Status: Gold Member Gold Member
Gosford NSW, Australia   aus
Member Since: 2006-06-18
Home Site: The MG Experience
Last Login: 2013-05-24 18:52:41
Forum Activity: 2013-05-24 22:25:55
Forum Posts: 4,203

Owner of '67 MGB in bits. *Update* Many more bits now and more to come! *Update2* Lots more bits and now on Rotisserie. *Update3* Started the way back has revamped front and rear suspension and is back on the ground. *Update* Pretty sure now car is a '66. *Update4* Did complete motor rebuild and it's in and running. Now working on the interior and the body. *Update5* Now road registered and able to be driven - still lots of cosmetic issues, however.

Personal Vehicle Registry

Chris W 1966 MG MGB Hermitage Burgundy

1966 MG MGB
"Basil"
YGHN32965
Chris W 1990 Nissan Patrol White

1990 Nissan Patrol
"(Patrol) The Beast"
JN100KY60A0022XXX

1992 Subaru Legacy
"(Liberty)"
JF2BC7CR0EH023XXX


3 Vehicles -- Total mileage: 345,000 mi (555,224 km) -- Average age: 1983

Member Journal – Chris Williams' Journal

There are 190 total entries in this Journal.
Showing summary of the most recent Journal entries:

Bit Of A Post Script.

Posted on: Monday April 29, 2013

I've put some miles on the car since the fix and all is going well -ish. I checked the head torque twice and I've re-checked the valve clearances. They are moving around and the valve train is still quite noisy. I'm not particularly concerned about the noise - better that way than too tight. I spent some time on the tune and found that it was horribly advanced. I dialled it back to about 15deg at idle and I found that idle speed dropped dramatically. It's now more in a suitable range just ...

The Fix! And Some Other Tales.

Posted on: Saturday April 6, 2013

Well, the bottom line is it's all good! I did some testing on the head before going to the trouble of cleaning and positioned it level and filled the combustion chambers with WD 40. After about an hour, which I spent doing the final cleanup of the block, there was virtually no evidence of the fluid leaking through so I concluded that the va...

Delivery From Moss.

Posted on: Monday April 1, 2013

Did not expect this so soon! The order from Moss UK arrived this morning and I was checking it out and realised that I'd missed ordering the head nuts and washers. DUH! Could make a supplementary order but I think I just get them locally. Gasket looks good - much better than the one I put on before. Got a nice 'sticky' feel to it and the junctions between 1&2 and 3&4 look much better. They have a piece of brass between the thin area which should help in dissipating heat from that area. ...

Back The The Main Event, The MGB Motor 'failure'

Posted on: Monday April 1, 2013

I'll jump straight in: Motor full rebuild 10k miles ago. I put it together myself . Suddenly developed a motor rattle and I had it towed home. Checked compression, 1 & 2 virtually no compression. Further investigation established almost certainly a leak from 1 to 2. Oil clear. Water clear. This was confirmed today after taking head off.



... and 186 more posts.

MG Experience Library Articles

Date Site Title Category Comments
2006-04-02 mgb KPH Speedometer Conversion Service:Electrical and Instruments 2

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