MG-2013 is only 58 days away! · Corvallis, OR · July 17–21, 2013 · Visit MG-2013.com or the MG-2013 Forum for more info

The 72B Mini Project

esd3104 Simon Dix
Simon Dix   usa  
O'Fallon MO, USA

Total Posts: 59 Latest Post: 2011-12-18 19:35:32
Follow new posts by subscribing to the   RSS Feed
Link to this journal: http://www.mgexp.com/journal/esd3104






Page :     1   .   2   .   3   .   4   .   5   .   6   .   7      Next →      [10]



Changing 72B Speedo

Simon Dix   usa — Posted on The MG Experience
Sunday December 18, 2011 7:35 PM
Just keeping track of the mileage due to a speedo swap.

Removing speedo reading 51,443 and replacing with 50,541


New on the left old on the right

New on the left, old on the right

New on the left old on the right

New on the left, old on the right




. You can hide this ad & support this site by upgrading to a Gold Membership ~ click here for more info.


Member Comments on this Journal Entry: Changing 72B Speedo   ↵

No comments have been posted yet...

Want to leave a comment or ask a question?
Please Sign In — or Register a new account (it's free!)

   





77B Compression Test Results

Simon Dix   usa — Posted on The MG Experience
Wednesday June 22, 2011 7:19 PM
June 22, 2011 - Compression Test relative to slight head gasket weeping above engine number plate.

Run 1 Before Retorque: #1=138, #2=125, #3=138, #4=140

After Retorque Run 2: #1=135, #2=132, #3=138, #4=140

Both tests done with throttle wide open.



Member Comments on this Journal Entry: 77B Compression Test Results   ↵

No comments have been posted yet...

Want to leave a comment or ask a question?
Please Sign In — or Register a new account (it's free!)

   





Fixing Oil Scraper Ring - 46,198

Simon Dix   usa — Posted on The MG Experience
Monday June 21, 2010 10:50 AM
Just to log that the mileage at the time I fixed the #4 piston oil scraper ring was 46,192 on the speedo.



Member Comments on this Journal Entry: Fixing Oil Scraper Ring - 46,198   ↵

No comments have been posted yet...

Want to leave a comment or ask a question?
Please Sign In — or Register a new account (it's free!)

   





Engine Rebuild

Simon Dix   usa — Posted on The MG Experience
Tuesday May 25, 2010 11:02 AM
Just to remind myself the engine rebuild went in at 43,886 reading on the speedo I switched over to for the 1000 TPM OD.



Member Comments on this Journal Entry: Engine Rebuild   ↵

No comments have been posted yet...

Want to leave a comment or ask a question?
Please Sign In — or Register a new account (it's free!)

   





Compression Test Results

Simon Dix   usa — Posted on The MG Experience
Sunday August 10, 2008 10:40 AM
Scarlett readings:
Compression Test Dry
#1 145
#2 160
#3 160
#4 160

Compression Test Wet
#1 165
#2 190
#3 185
#4 190

Subsequent Cam/Intake Exhaust Port Tests in .001's

Ex #1 148
In #2 265
In #3 255
Ex #4 260
Ex #5 194
In #6 239
In #7 265
Ex #8 260

While I was at it dry compression on Tigger was

#1 130
#2 130
#3 128
#4 130


Concern after Valve Adj 1 Not Compressing valve

Concern after Valve Adj - #1 Not Compressing valve Spring

Other for comparision cam issue probably

Other for comparision - cam issue? probably




. You can hide this ad & support this site by upgrading to a Gold Membership ~ click here for more info.


Member Comments on this Journal Entry: Compression Test Results   ↵

No comments have been posted yet...

Want to leave a comment or ask a question?
Please Sign In — or Register a new account (it's free!)

   





OK so I needed to clean up the console wiring and so I routed the hazard light harness and cigarette harness through the lower hole in the metal frame of the console on the drivers’ side. I wasn’t sure how everything would connect up but it all seemed to work. So, despite the many other things that need doing, I decided to install my stereo.

Having reviewed the wiring diagram I planned to connect the permanent power lead to the purple wiring, the switched power to the green/pink and ground to one of the ground connectors. Using the connectors for the stereo means I need to rethink the wiring of the console light but that will take some more thinking. I wanted to check the stereo out as I bought it a while back and hadn’t even plugged it in.

I used wires from my old wiring harness to match the wires I planned to connect to so that gave me the bullet connectors I would need and I used male & female connectors to join the stereo wires to the wire from the old harness. I did a quick trial run and everything worked, as soon as I remembered to turn on the ignition key, Doh! Since this worked I started to install the holding bracket and found that the hole was about 1/8th inch too small. So I opened it up a little with a Stanley knife and that worked nicely and the bracket fit. After some adjusting of wires I got the stereo to fully sit back into the bracket. It’s a tight fit and the back of the unit presses a little on the heater hoses but nothing too terrible.

Then I did some wire clean up and connected up the 6x9 speakers that I had installed into my speaker boxes and finally got to test the sounds. Sweet! A little more wire tidying up and that will do for the day.


Got some tunes installed and operational There

Got some tunes installed and operational. There’s a rats nest of wires behind there but it works.




Member Comments on this Journal Entry: More Centre Console – Stereo Installation Done (Mostly)   ↵

No comments have been posted yet...

Want to leave a comment or ask a question?
Please Sign In — or Register a new account (it's free!)

   



Page :     1   .   2   .   3   .   4   .   5   .   6   .   7      Next →      [10]

Join Our Club

Sign In to post questions or share your photos!

MGExp Menu

Welcome

Forums

Journals ->

Top Journals

Latest Posts

Browse All

Calendar

Membership

Tech Library

Car Registry

Cars For Sale

Model Info

Motorsport

Directory

Member Map

MGExp Store

Search

Advertising Info

Smartphone quick link
mgexp.mobi

Adjust Text Size

Larger Smaller
Reset Save